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218a940eda
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reordered a bit advance, ids and phi data. Also working 504012 version with pwm and phi controllers
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2026-04-30 18:33:19 +02:00 |
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d95e4e18f1
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424026 working with pwm and phi. Rpm filtered for acceleration compensation still missing. Only using phi_ad and applying our accel comp
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2026-04-30 15:03:57 +02:00 |
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5e20601eeb
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Fixed the closed loop oscillation, PI integrator was to hard, also wrong interpolation algo. Its being tested in car, supposedly should be validated and put into release. 504012
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2026-04-27 22:03:00 +02:00 |
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0c90da4cfb
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Whole advance control system overhaul. Target angle is now calculated entirely like OEM firmware. Calibration data is fully parsed from a rom dump and a proper file is created with a python extraction tool. Open loop is tested and generates same values as original. In car PID testing has not been done.Voltage compensation is not active as we dont have that parameter's acquisition. 0130 used as flag couldnt be properly decompiled, but logging the ram shows its never blocking the closed loop state. Bench testing is required for verification. Some parameter called setpoint_offset hasnt yet been decompiled, and extractin is through RAM reading. Also modified can_db for T06301 cfgs to include proper FBNW acquisiton
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2026-04-17 23:32:40 +02:00 |
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02787c3e34
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Full kline refactor, passes 815 verification initialization
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2026-04-10 12:19:58 +02:00 |
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b43177774e
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Added k-line files from 1.9 version, works until dfi
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2026-03-30 21:33:37 +02:00 |
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64adb64c81
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Initial port
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2026-03-30 18:36:35 +02:00 |
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